During summer 2023 and right through to the end of the year, I had a very perplexing problem with my 2003 Mercury 115 4-stroke (on my 160 Dauntless). I didn't post here looking for help since it wasn't strictly Whaler-related; instead I had a running thread on thehulltruth.com where I got lots of input. Some of it was even useful! But I wanted to relate the story here just in case it proves helpful to anyone else.
Starting in the early summer, my engine would occasionally "cut out" at cruise speeds. At first it was just a little blip, almost too quick to notice. I'd describe it as if I'd very quickly turned off the ignition and turned it back on. As summer went on, the problem became more pronounced, with the engine sometimes running very roughly for a few seconds before smoothing out again. The problem didn't really seem to be related to anything in particular, other than I was always running at planing speed. I checked the ignition switch and the kill switch, but both seemed to work fine.
Although intuitively it seemed more like an ignition problem to me, I replaced both the large cartridge fuel filter as well as the small filter that this engine has under the cowling right next to the low-pressure fuel pump, but to no effect. During September the engine would suddenly no longer run above a fast idle. Pushing the throttle up would simple cause it to quite abruptly die at around 2500 RPM.
I started my trouble-shooting in earnest and tried to check all the sensors with an ohmmeter. I did find that the throttle position sensor (TPS) was very noisy (that is, the change in resistance was not smooth) and that seemed like a very plausible culprit. But while the TPS was demonstrably bad, replacing it didn't help. At this point I also checked the fuel rail pressure which read a steady 42 PSI, which eliminated the high-pressure fuel pump and the vapor separator tank as a likely problem.
This engine actually has the Yamaha F115 powerhead (during the early 2000s Mercury bought 75-115 and 225 HP powerheads from Yamaha while they worked on developing their own) and there's a diagnostic connector where you can hook up an indicator lamp. The intent is that the lamp will blink codes at you. All I ever got was one long flash when the engine died, which wasn't even a documented code. I did have to jury-rig my own connector (the factory connector is no longer available new) so I thought perhaps I didn't have the pinouts correct. At that point it didn't seem like there was really anything else I could do, so I took the boat to a local shop. They had the boat for 3 weeks, then told me all it needed was some new spark plugs. They also managed to scratch my freshly-repainted cowling which was quite annoying. Naturally, when I got the boat back it still didn't run. Clearly they're not the top mechanics here at the lake, but the experience did reinforce my desire to fix it myself.
Given that the engine was now starting but then shutting down within 10-20 seconds, my suspicion next went to the manifold absolute pressure (MAP) sensor. This engine doesn't have a mass airflow (MAF) sensor, instead it estimates the intake airflow based on the TPS, the MAP pressure reading, and the intake air temperature sensor. It seemed like if the sensor was bad, then perhaps the engine control module (ECM) would let the engine start but then shut it down when the manifold pressure wasn't seen to be dropping. The MAP sensor was a bit pricey, and you can probably anticipate that it didn't fix the problem either.
One important thing I did learn in the thehulltruth.com discussion was that the Yamaha computer-based diagnostic system does work on this engine, so I bought it on eBay and received the software as well as an OBD-II reader and an adapter cable to fit the engine's diagnostic connector. The diagnostic system turned out to be critically important, just not in the way that I was expecting. What I learned was that when the engine died, the connection to the ECM died with it. This led me to conclude that the ECM itself was shutting down, though I had no idea why. The main relay was a possible cause, so I temporarily jumpered the connectors to simulate the relay connections staying closed, but to no effect.
I brought in a neighbor who's a classic sports car guy, and his thoughts went right to the voltage regulator. I'd replaced the voltage regulator around mid-summer when I noticed the system voltage was hanging around 12 V and there seemed to be no charging current. Given that I had a brand-new OEM voltage regulator, I thought the odds of that being a problem were just about zero. But as a first test, I simply unplugged the voltage regulator. Well what do you know, the engine ran perfectly. I bench-tested the voltage regulator and determined that the rectifier diodes were working properly, but I couldn't do a very good test of the voltage output since the engine wouldn't run for more than a few seconds at a time. With the regulator disconnected, I checked continuity and voltage output from the stator coils and they were within spec. My hypothesis was that perhaps some AC voltage was leaking through the voltage regulator and freaking out the ECM.
I bought a new voltage regulator (this time a cheap after-market version for 1/5 the price) but to my surprise the engine still started up and then died. It ran for a bit longer, maybe 30-40 seconds, but overall the result was the same. I was glad I only spent $30! With the engine running just a little bit longer, I was able to see that the rest voltage at the engine was about 12.5 V, dropping to 11.0 or so during the start, then continually climbing until the engine stopped. The maximum that I was able to measure was 15.0-15.5 V. That's unusually high for a nominally 12 V system, which should have a charging voltage of around 13.7-14.2 V. Perhaps the ECM was shutting down due to over-voltage protection?
While examining the SELOC manual for the 1000th time, I came across a description of the voltage regulator that said something like "when the battery voltage is at the normal charging voltage, the voltage regulator shunts excess power to ground." I know this is an overly-simplistic explanation, but I sat bolt upright -- if the voltage regulator ground was bad, it wouldn't be able to "shunt excess power" which could result in an over-voltage condition! I pulled off the voltage regulator ground connector (which was shared with the ECM ground) and it looked fine. This may be a 21-year-old engine, but it's primarily freshwater and it's super-clean. Nevertheless I polished up the engine block land, both sides of the ring terminals, and the bolt itself with 300-grit sandpaper and put it all back together. The engine idled perfectly. I put the boat back in the water and she ran great from idle all the way up to wide-open throttle.
I spent the better part of 4 months chasing this problem, spent $500 on parts I didn't really need, and ultimately solved it in 5 minutes with a piece of sandpaper. Lesson learned: check your ground connections.
-Bob
A Long Story of an InterestingProblem with a 2003 Mercury 115 4-Stroke Engine
- GoldenDaze
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A Long Story of an InterestingProblem with a 2003 Mercury 115 4-Stroke Engine
2003 160 Dauntless Golden Daze (2003-2024)
2023 EdgeWater 230CC Havin' a Ball (2024-...)
2023 EdgeWater 230CC Havin' a Ball (2024-...)
Re: A Long Story of an InterestingProblem with a 2003 Mercury 115 4-Stroke Engine
BOB--thanks for posting your narrative of how you found the problem with the intermittent cutting-out of your 2003 Mercury 115-HP four-stroke-power-cycle. Finding the cause of that electrical problem was quite an accomplishment.
Regarding electrical connections in a low-voltage system like a 12-Volt system, your description of the appearance of the ground circuit from the voltage regulator to the engine chassis was very interesting.
I have commented before that in working with low-voltage circuits, the existence of just a very thin layer of oxidation at a connection can interrupt the flow of current. At low voltage, an electrical discontinuity can be created and be so thin that you cannot notice it by visual inspection. A connection may have very normal appearance, but not be connected at all electrically.
The initial circumstance when this problem appeared were, in hindsight, also indicating the root cause: as the engine speed increased, the voltage being produced by the alternator was also increasing. The voltage regulator was then trying to operate as intended, and regulate the now too-high voltage output by shunting current to ground. When the path to ground was no longer available, the engine control module must have decided it had to protect itself and shut off the engine. However, it seems odd that eventually the problem worsened to the point that the engine would even sustain operation at lower engine speeds. This could be explained by a change in the resistance at the poor ground connection. At first, perhaps the connection was not completely an open circuit, just a connection whose resistance was much higher than it should have been. At lower speeds, and thus at lower alternator voltage output, the connection was just good enough to maintain the needed shunting current for the voltage regulator to operate normally. Over time, the connection worsened, and eventually became such a high resistance that even at engine idle speeds the voltage regulator could not keep the alternator voltage under control.
Regarding electrical connections in a low-voltage system like a 12-Volt system, your description of the appearance of the ground circuit from the voltage regulator to the engine chassis was very interesting.
I have commented before that in working with low-voltage circuits, the existence of just a very thin layer of oxidation at a connection can interrupt the flow of current. At low voltage, an electrical discontinuity can be created and be so thin that you cannot notice it by visual inspection. A connection may have very normal appearance, but not be connected at all electrically.
The initial circumstance when this problem appeared were, in hindsight, also indicating the root cause: as the engine speed increased, the voltage being produced by the alternator was also increasing. The voltage regulator was then trying to operate as intended, and regulate the now too-high voltage output by shunting current to ground. When the path to ground was no longer available, the engine control module must have decided it had to protect itself and shut off the engine. However, it seems odd that eventually the problem worsened to the point that the engine would even sustain operation at lower engine speeds. This could be explained by a change in the resistance at the poor ground connection. At first, perhaps the connection was not completely an open circuit, just a connection whose resistance was much higher than it should have been. At lower speeds, and thus at lower alternator voltage output, the connection was just good enough to maintain the needed shunting current for the voltage regulator to operate normally. Over time, the connection worsened, and eventually became such a high resistance that even at engine idle speeds the voltage regulator could not keep the alternator voltage under control.
- GoldenDaze
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Re: A Long Story of an InterestingProblem with a 2003 Mercury 115 4-Stroke Engine
initial circumstance when this problem appeared were, in hindsight, also indicating the root cause
Exactly! All along I was searching for something that tied all the progressing symptoms together, and I was never really satisfied that I had the right answer with the TPS or MAP sensors. The over-voltage finally tied the whole year together.
By the way, the new voltage regulator that I installed earlier in the year (an expensive OEM one) turned out to be just fine, so it's back on the engine. The "problem" with that one was that it raised the voltage too fast for me to see the pattern with my voltmeter. The cheap aftermarket one brought the voltage up more slowly, so in a way -- like the diagnostic system -- it was critical to the solution, just not in the way I expected.
2003 160 Dauntless Golden Daze (2003-2024)
2023 EdgeWater 230CC Havin' a Ball (2024-...)
2023 EdgeWater 230CC Havin' a Ball (2024-...)
Re: A Long Story of an InterestingProblem with a 2003 Mercury 115 4-Stroke Engine
That is quite a twist in the plot.GoldenDaze wrote:...The "problem" with [the OEM voltage regulator] was that it raised the voltage too fast for me to see the pattern with my voltmeter. The cheap aftermarket one brought the voltage up more slowly, so in a way -- like the diagnostic system -- it was critical to the solution, just not in the way I expected.
Re: A Long Story of an InterestingProblem with a 2003 Mercury 115 4-Stroke Engine
Which parts [were involved in the solution of the problem]? Can you provide a diagram? Can you provide photographs?
I also have a 2003 Mercury 115 FOURSTROKE engine. It is doing the exact same thing [as the engine discussed in this thread]. I would like to [try to fix the problem myself] as our dealer was unable to fix the problem.
I also have a 2003 Mercury 115 FOURSTROKE engine. It is doing the exact same thing [as the engine discussed in this thread]. I would like to [try to fix the problem myself] as our dealer was unable to fix the problem.
- GoldenDaze
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Re: A Long Story of an InterestingProblem with a 2003 Mercury 115 4-Stroke Engine
beul wrote:I also have a 2003 Mercury 115 FOURSTROKE engine. It is doing the exact same thing [as the engine discussed in this thread]. I would like to [try to fix the problem myself] as our dealer was unable to fix the problem.
Hi Bill, I sold the boat and engine last year, so I no longer have the manual. But the remedy to the problem was pretty simple: if you remove the intake silencer and the voltage regulator, then you'll find (as I recall) three bolts that attach ground wires to the block. Each of them has 2 or 3 ring terminals under the bolt head. I sanded the engine block surface under the bolts, the underside of the bolt faces, and both sides of each ring terminal.
Good luck and I hope this fixes your problem.
-Bob
2003 160 Dauntless Golden Daze (2003-2024)
2023 EdgeWater 230CC Havin' a Ball (2024-...)
2023 EdgeWater 230CC Havin' a Ball (2024-...)
Re: A Long Story of an InterestingProblem with a 2003 Mercury 115 4-Stroke Engine
BOB--thanks again for the added details of the location of the multiple electrical negative circuit conductor connections to the engine block that were suspected to be bad connections, how they were not easily seen due to being obscured behind other engine components, and how you improved the connections by using abrasion of the contact surfaces.
RECOMMENDATION
A good way to enhance electrical connections that are suspected to have some corrosion is to carefully wet sand those surfaces, using emery cloth sand paper of about 400-grit and WD-40 as the wetting agent. After wet sanding, wipe off any excess WD-40 with a clean rag. Using fine grit is important. Coarse grit sanding will create a rough surface, which is just the sort of surface where corrosion can take hold.
The reason I use WD-40 is its known ability to restore electrical connection. It is widely thought that kerosene or a similar light oil is the base ingredient, so the fluid will tend to evaporate with some drying time if not applied excessively.
Also, once the electrical connections are restored, are completely dry, and are known to be making proper connection, a good practice to help prevent future corrosion is to spray the connections with a sealing aerosol spray, such as BOESHIELD T-9 aerosol rust and corrosion protection.
The reason I use BOESHIELD T-9 is it dries nicely, and unlike a grease it won’t tend to capture and hold dirt.
On some Mercury engines I have seen black paint (similar to the or perhaps the same) paint that is used to paint the engine block) sprayed onto electrical connections to the engine block, but I don’t like that approach; to investigate the connection requires getting off the paint, which is tedious and tiresome.
RECOMMENDATION
A good way to enhance electrical connections that are suspected to have some corrosion is to carefully wet sand those surfaces, using emery cloth sand paper of about 400-grit and WD-40 as the wetting agent. After wet sanding, wipe off any excess WD-40 with a clean rag. Using fine grit is important. Coarse grit sanding will create a rough surface, which is just the sort of surface where corrosion can take hold.
The reason I use WD-40 is its known ability to restore electrical connection. It is widely thought that kerosene or a similar light oil is the base ingredient, so the fluid will tend to evaporate with some drying time if not applied excessively.
Also, once the electrical connections are restored, are completely dry, and are known to be making proper connection, a good practice to help prevent future corrosion is to spray the connections with a sealing aerosol spray, such as BOESHIELD T-9 aerosol rust and corrosion protection.
The reason I use BOESHIELD T-9 is it dries nicely, and unlike a grease it won’t tend to capture and hold dirt.
On some Mercury engines I have seen black paint (similar to the or perhaps the same) paint that is used to paint the engine block) sprayed onto electrical connections to the engine block, but I don’t like that approach; to investigate the connection requires getting off the paint, which is tedious and tiresome.
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Re: A Long Story of an InterestingProblem with a 2003 Mercury 115 4-Stroke Engine
Great story and I can relate too, because I also have almost the same engine: a 90-HP Yamaha-built four-stroke-poewr-cycle model. Your description of the voltage regulator and its location and such is spot on with mine.
To see these engines are still kicking is nice.
My voltage regulator story is that mine caught fire--well sorta. The insulation cracked off of some of the voltage regulator wiring and they they shorted against each other. causing the remaining wire insulation to catch fire.
At low engine speed and idle, [the regulator] was not shunting much [current] to ground, and we took a long ride back to the ramp at low RPM.
I ended up buying an OEM voltage regulator, but a used one from eBay. It works a treat.
Reflecting back on it, I wonder if my voltage regulator fire occurred due to the same ground connection problems you had, that is, there was too much resistance built up and that caused the wires to overheat.
The engine was on was a saltwater boat since new in 2000 until I took it fresh-only in 2012.
-Peter
To see these engines are still kicking is nice.
My voltage regulator story is that mine caught fire--well sorta. The insulation cracked off of some of the voltage regulator wiring and they they shorted against each other. causing the remaining wire insulation to catch fire.
At low engine speed and idle, [the regulator] was not shunting much [current] to ground, and we took a long ride back to the ramp at low RPM.
I ended up buying an OEM voltage regulator, but a used one from eBay. It works a treat.
Reflecting back on it, I wonder if my voltage regulator fire occurred due to the same ground connection problems you had, that is, there was too much resistance built up and that caused the wires to overheat.
The engine was on was a saltwater boat since new in 2000 until I took it fresh-only in 2012.
-Peter
Re: A Long Story of an InterestingProblem with a 2003 Mercury 115 4-Stroke Engine
Generally heat in an electrical circuit is created by the flow of too much current, which tends to occur when there is too little resistance.pcrussell50 wrote:...I wonder if my voltage regulator fire occurred due to the same ground connection problems you had, that is, there was too much resistance built up and that caused the wires to overheat.
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- Joined: Fri Oct 16, 2015 1:08 am
- Location: SoCal/SoNev
Re: A Long Story of an InterestingProblem with a 2003 Mercury 115 4-Stroke Engine
jimh wrote:Generally heat in an electrical circuit is created by the flow of too much current, which tends to occur when there is too little resistance.pcrussell50 wrote:...I wonder if my voltage regulator fire occurred due to the same ground connection problems you had, that is, there was too much resistance built up and that caused the wires to overheat.
What I meant, (and probably failed), to convey is that I thought my regulator fire was due to old insulation cracking off and causing a short. Now, after the story in this thread, I wonder if the real culprit was the same situation as the OP, with the same ground.
-Peter.
Re: A Long Story of an InterestingProblem with a 2003 Mercury 115 4-Stroke Engine
If one wire in the bundles connecting to the engine chassis ground from the voltage regulator had a poor connection to ground and it shorted to another wire in the same or in another bundle with a good ground, then more current would flow into the other conductor with the good ground for that short distance between where the short occurred and the chassis than normally would exist on that conductor. Would that be enough added current to create enough heat to reach combustion for the insulation?
To me it seems more likely that a conductor that was not supposed to be in contact with ground shorted to a conductor carrying ground. That would create a high current flow and create heat.
I don’t know any specifics of the voltage regulator on the Mercury engines of that era, but the general vibe is the electrical parts were made in Mexico and could exhibit a shorter service life that the engine owner might have anticipated.
The situation is like alternators on GM cars. Their capacity is about one electron greater what the engine and vehicle need. I used to own a lot of GM cars and I have replaced the alternator in three different models over the years.
To me it seems more likely that a conductor that was not supposed to be in contact with ground shorted to a conductor carrying ground. That would create a high current flow and create heat.
I don’t know any specifics of the voltage regulator on the Mercury engines of that era, but the general vibe is the electrical parts were made in Mexico and could exhibit a shorter service life that the engine owner might have anticipated.
The situation is like alternators on GM cars. Their capacity is about one electron greater what the engine and vehicle need. I used to own a lot of GM cars and I have replaced the alternator in three different models over the years.